2024-07-23T00:42:52.259Z,1721695372.259 [CommandExec](IMPORTANT): got command restart logs 2024-07-23T00:42:52.692Z,1721695372.692 [OnDock:M.Docked](IMPORTANT): No IP address on dock subnet, restarting DHCP 2024-07-23T00:43:03.284Z,1721695383.284 [CommandExec](IMPORTANT): got command ! /mnt/mmc/LRAUV/Tools/dhcp.sh 2024-07-23T00:43:04.139Z,1721695384.139 [CommandExec](IMPORTANT): /mnt/mmc/started/2024-07-23UTC004304_sh 2024-07-23T00:49:39.088Z,1721695779.088 [CommandExec](IMPORTANT): got command docking standby 2024-07-23T00:49:39.088Z,1721695779.088 [CommandExec](IMPORTANT): Switching docking moudle to STANDBY. 2024-07-23T01:12:51.393Z,1721697171.393 [CommandExec](IMPORTANT): got command ! ifconfig 2024-07-23T01:12:51.611Z,1721697171.611 [CommandExec](IMPORTANT): eth0 Link encap:Ethernet HWaddr 50:2D:F4:07:45:4B UP BROADCAST RUNNING MULTICAST MTU:1500 Metric:1 RX packets:3594 errors:0 dropped:0 overruns:0 frame:0 TX packets:4787 errors:0 dropped:0 overruns:0 carrier:0 collisions:23 txqueuelen:1000 RX bytes:795552 (776.9 Kb) TX bytes:880484 (859.8 Kb) Interrupt:29 lo Link encap:Local Loopback inet addr:127.0.0.1 Mask:255.0.0.0 UP LOOPBACK RUNNING MULTICAST MTU:16436 Metric:1 RX packets:719 errors:0 dropped:0 overruns:0 frame:0 TX packets:719 errors:0 dropped:0 overruns:0 carrier:0 collisions:0 txqueuelen:0 RX bytes:60496 (59.0 Kb) TX bytes:60496 (59.0 Kb) 2024-07-23T01:42:52.314Z,1721698972.314 [CommandExec](IMPORTANT): got command ! ifconfig 2024-07-23T01:42:52.483Z,1721698972.483 [CommandExec](IMPORTANT): eth0 Link encap:Ethernet HWaddr 50:2D:F4:07:45:4B UP BROADCAST RUNNING MULTICAST MTU:1500 Metric:1 RX packets:3594 errors:0 dropped:0 overruns:0 frame:0 TX packets:4971 errors:0 dropped:0 overruns:0 carrier:0 collisions:23 txqueuelen:1000 RX bytes:795552 (776.9 Kb) TX bytes:989044 (965.8 Kb) Interrupt:29 lo Link encap:Local Loopback inet addr:127.0.0.1 Mask:255.0.0.0 UP LOOPBACK RUNNING MULTICAST MTU:16436 Metric:1 RX packets:719 errors:0 dropped:0 overruns:0 frame:0 TX packets:719 errors:0 dropped:0 overruns:0 carrier:0 collisions:0 txqueuelen:0 RX bytes:60496 (59.0 Kb) TX bytes:60496 (59.0 Kb) 2024-07-23T02:12:52.754Z,1721700772.754 [OnDock:Detach:A](IMPORTANT): Mission ending, breaking off. Range: 1.900000 m . 2024-07-23T02:12:53.171Z,1721700773.171 [CommandExec](IMPORTANT): got command ! ifconfig 2024-07-23T02:12:53.336Z,1721700773.336 [CommandExec](IMPORTANT): eth0 Link encap:Ethernet HWaddr 50:2D:F4:07:45:4B UP BROADCAST RUNNING MULTICAST MTU:1500 Metric:1 RX packets:3594 errors:0 dropped:0 overruns:0 frame:0 TX packets:5156 errors:0 dropped:0 overruns:0 carrier:0 collisions:23 txqueuelen:1000 RX bytes:795552 (776.9 Kb) TX bytes:1098194 (1.0 Mb) Interrupt:29 lo Link encap:Local Loopback inet addr:127.0.0.1 Mask:255.0.0.0 UP LOOPBACK RUNNING MULTICAST MTU:16436 Metric:1 RX packets:719 errors:0 dropped:0 overruns:0 frame:0 TX packets:719 errors:0 dropped:0 overruns:0 carrier:0 collisions:0 txqueuelen:0 RX bytes:60496 (59.0 Kb) TX bytes:60496 (59.0 Kb) 2024-07-23T02:13:36.141Z,1721700816.141 [DockingStepper](FAULT): uart error - getPosition..serial timeout 2024-07-23T02:13:45.307Z,1721700825.307 [DockingStepper](FAULT): Command Overflow Error 2024-07-23T02:13:45.307Z,1721700825.307 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:14:45.593Z,1721700885.593 [OnDock:Detach:B.Undock](IMPORTANT): Undocking sequence complete. 2024-07-23T02:14:45.977Z,1721700885.977 [MissionManager](IMPORTANT): Started mission DefaultWithUndock 2024-07-23T02:15:46.651Z,1721700946.651 [DockingStepper](FAULT): Command Overflow Error 2024-07-23T02:15:46.651Z,1721700946.651 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:15:52.662Z,1721700952.662 [DefaultWithUndock:LeaveDock:B.Undock](IMPORTANT): Undocking sequence complete. 2024-07-23T02:15:59.718Z,1721700959.718 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:20:24.609Z,1721701224.609 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:21:22.450Z,1721701282.450 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:23:03.583Z,1721701383.583 [DockingStepper](FAULT): uart error - getPosition..serial buffer full 2024-07-23T02:29:45.612Z,1721701785.612 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:31:15.914Z,1721701875.914 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:31:44.657Z,1721701904.657 [DockingStepper](FAULT): Docking arm not reporting position 2024-07-23T02:31:45.834Z,1721701905.834 [DefaultWithUndock:SurfaceDefault:CheckIn:E](IMPORTANT): Default mission has been running for 16.992061 min